Search results for: GE Bently Nevada
Commenced in January 2007
Frequency: Monthly
Edition: International
Paper Count: 9

Search results for: GE Bently Nevada

9 Diagnosis of Intermittent High Vibration Peaks in Industrial Gas Turbine Using Advanced Vibrations Analysis

Authors: Abubakar Rashid, Muhammad Saad, Faheem Ahmed

Abstract:

This paper provides a comprehensive study pertaining to diagnosis of intermittent high vibrations on an industrial gas turbine using detailed vibrations analysis, followed by its rectification. Engro Polymer & Chemicals Limited, a Chlor-Vinyl complex located in Pakistan has a captive combined cycle power plant having two 28 MW gas turbines (make Hitachi) & one 15 MW steam turbine. In 2018, the organization faced an issue of high vibrations on one of the gas turbines. These high vibration peaks appeared intermittently on both compressor’s drive end (DE) & turbine’s non-drive end (NDE) bearing. The amplitude of high vibration peaks was between 150-170% on the DE bearing & 200-300% on the NDE bearing from baseline values. In one of these episodes, the gas turbine got tripped on “High Vibrations Trip” logic actuated at 155µm. Limited instrumentation is available on the machine, which is monitored with GE Bently Nevada 3300 system having two proximity probes installed at Turbine NDE, Compressor DE &at Generator DE & NDE bearings. Machine’s transient ramp-up & steady state data was collected using ADRE SXP & DSPI 408. Since only 01 key phasor is installed at Turbine high speed shaft, a derived drive key phasor was configured in ADRE to obtain low speed shaft rpm required for data analysis. By analyzing the Bode plots, Shaft center line plot, Polar plot & orbit plots; rubbing was evident on Turbine’s NDE along with increased bearing clearance of Turbine’s NDE radial bearing. The subject bearing was then inspected & heavy deposition of carbonized coke was found on the labyrinth seals of bearing housing with clear rubbing marks on shaft & housing covering at 20-25 degrees on the inner radius of labyrinth seals. The collected coke sample was tested in laboratory & found to be the residue of lube oil in the bearing housing. After detailed inspection & cleaning of shaft journal area & bearing housing, new radial bearing was installed. Before assembling the bearing housing, cleaning of bearing cooling & sealing air lines was also carried out as inadequate flow of cooling & sealing air can accelerate coke formation in bearing housing. The machine was then taken back online & data was collected again using ADRE SXP & DSPI 408 for health analysis. The vibrations were found in acceptable zone as per ISO standard 7919-3 while all other parameters were also within vendor defined range. As a learning from subject case, revised operating & maintenance regime has also been proposed to enhance machine’s reliability.

Keywords: ADRE, bearing, gas turbine, GE Bently Nevada, Hitachi, vibration

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8 Evaluation of the Effectiveness of a HAWK Signal on Compliance in Las Vegas Nevada

Authors: A. Paz, M. Khadka, N. Veeramisti, B. Morris

Abstract:

There is a continuous large number of crashes involving pedestrians in Nevada despite the numerous safety mechanisms currently used at roadway crossings. Hence, additional as well as more effective mechanisms are required to reduce crashes in Las Vegas, in particular, and Nevada in general. A potential mechanism to reduce conflicts between pedestrians and vehicles is a High-intensity Activated crossWalK (HAWK) signal. This study evaluates the effects of such signals at a particular site in Las Vegas. Video data were collected using two cameras, facing the eastbound and westbound traffic. One week of video data before and after the deployment of the signal were collected to capture the behavior of both pedestrians and drivers. T-test analyses of pedestrian waiting time at the curb, curb-to-curb crossing time, total crossing time, jaywalking events, and near-crash events show that the HAWK system provides significant benefits.

Keywords: pedestrian crashes, HAWK signal, traffic safety, pedestrian danger index

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7 Screening Microalgae Strains Which Were Isolated from Agriculture and Municipal Wastewater Drain, Reno, Nevada and Reuse of Effluent Water from Municipal Wastewater Treatment Plant in Microalgae Cultivation for Biofuel Feedstock

Authors: Nita Rukminasari

Abstract:

The aim of this study is to select microalgae strains, which were isolated from agriculture and municipal wastewater drain, Reno, Nevada that has highest growth rate and lipid contents. The experiments in this study were carried out in two consecutive stages. The first stage is aimed at testing the survival capability of all isolated microalgae strains and determining the best candidates to grow in centrate cultivation system. The second stage was targeted at determination the highest growth rate and highest lipid content of the selected top performing algae strain when cultivated on centrate wastewater. 26 microalgae strains, which were isolated from municipal and agriculture waste water, were analyzed using Flow cytometer for FACS of lipid with BODIPY and Nile Red as a lipid dyes and they grew on 96 wells plate for 31 days to determine growth rate as a based line data for growth rate. The result showed that microalgae strains which showed a high mean of fluorescence for BODIPY and Nile Red were F3.BP.1, F3.LV.1, T1.3.1, and T1.3.3. Five microalgae strains which have high growth rate were T1.3.3, T2.4.1. F3.LV.1, T2.12.1 and T3.3.1. In conclusion, microalgae strain which showed the highest starch content was F3.LV.1. T1.3.1 had the highest mean of fluorescence for Nile Red and BODIPY. Microalgae strains were potential for biofuel feedstock such as F3.LV.1 and T1.3.1, those microalgae strains showed a positive correlation between growth rate at stationary phase, biomass and meant of fluorescence for Nile Red and BODIPY.

Keywords: agriculture and municipal wastewater, biofuel, centrate, microalgae

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6 The Relationship between the Epithermal Mineralization, Thermalism, and Basement Faults in the Region of Guelma: NE of Algeria

Authors: B. Merdas

Abstract:

The Guelma region constitutes a vast geothermal field whose local geothermal gradient is very high. Indeed, various thermal and thermo sources emerging in the region, including some at relatively high temperatures. In the mio Pliocene Hammam N'bails, basin emerges a hot spring that leaves develop a thick series of thermal travertine linked to it. Near the thermal emergences has settled a very special mineralization antimony and zinc and lead. The results of analyses of the thermal waters of the source of Hammam N'bails and the associated travertine, show abnormal values in Pb, Sb, Zn, As, and other metals, demonstrating the genetic link between those waters and mineralization. Hammam N'bails mineralizations by their mineral assembling represented and their association with the hot springs, are very similar to epithermal deposits with precious metals (gold and silver) like Senator mine in Turkey or ‘Carlin-type’ in Nevada (USA).

Keywords: hot springs, mineralization; basement faults, Guelma, NE Algeria

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5 1-g Shake Table Tests to Study the Impact of PGA on Foundation Settlement in Liquefiable Soil

Authors: Md. Kausar Alam, Mohammad Yazdi, Peiman Zogh, Ramin Motamed

Abstract:

The liquefaction-induced ground settlement has caused severe damage to structures in the past decades. However, the amount of building settlement caused by liquefaction is directly proportional to the intensity of the ground shaking. To reduce this soil liquefaction effect, it is essential to examine the influence of peak ground acceleration (PGA). Unfortunately, limited studies have been carried out on this issue. In this study, a series of moderate scale 1g shake table experiments were conducted at the University of Nevada Reno to evaluate the influence of PGA with the same duration in liquefiable soil layers. The model is prepared based on a large-scale shake table with a scaling factor of N = 5, which has been conducted at the University of California, San Diego. The model ground has three soil layers with relative densities of 50% for crust, 30% for liquefiable, and 90% for dense layer, respectively. In addition, a shallow foundation is seated over an unsaturated crust layer. After preparing the model, the input motions having various peak ground accelerations (i.e., 0.16g, 0.25g, and 0.37g) for the same duration (10 sec) were applied. Based on the experimental results, when the PGA increased from 0.16g to 0.37g, the foundation increased from 20 mm to 100 mm. In addition, the expected foundation settlement based on the scaling factor was 25 mm, while the actual settlement for PGA 0.25g for 10 seconds was 50 mm.

Keywords: foundation settlement, liquefaction, peak ground acceleration, shake table test

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4 Modified Clusterwise Regression for Pavement Management

Authors: Mukesh Khadka, Alexander Paz, Hanns de la Fuente-Mella

Abstract:

Typically, pavement performance models are developed in two steps: (i) pavement segments with similar characteristics are grouped together to form a cluster, and (ii) the corresponding performance models are developed using statistical techniques. A challenge is to select the characteristics that define clusters and the segments associated with them. If inappropriate characteristics are used, clusters may include homogeneous segments with different performance behavior or heterogeneous segments with similar performance behavior. Prediction accuracy of performance models can be improved by grouping the pavement segments into more uniform clusters by including both characteristics and a performance measure. This grouping is not always possible due to limited information. It is impractical to include all the potential significant factors because some of them are potentially unobserved or difficult to measure. Historical performance of pavement segments could be used as a proxy to incorporate the effect of the missing potential significant factors in clustering process. The current state-of-the-art proposes Clusterwise Linear Regression (CLR) to determine the pavement clusters and the associated performance models simultaneously. CLR incorporates the effect of significant factors as well as a performance measure. In this study, a mathematical program was formulated for CLR models including multiple explanatory variables. Pavement data collected recently over the entire state of Nevada were used. International Roughness Index (IRI) was used as a pavement performance measure because it serves as a unified standard that is widely accepted for evaluating pavement performance, especially in terms of riding quality. Results illustrate the advantage of the using CLR. Previous studies have used CLR along with experimental data. This study uses actual field data collected across a variety of environmental, traffic, design, and construction and maintenance conditions.

Keywords: clusterwise regression, pavement management system, performance model, optimization

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3 Alleviation of Thermal Stress in Pinus ponderosa by Plant-Growth Promoting Rhizobacteria Isolated from Mixed-Conifer Forests

Authors: Kelli G. Thorup, Kristopher A. Blee

Abstract:

Climate change enhances the occurrence of extreme weather: wildfires, drought, rising summer temperatures, all of which dramatically decline forest growth and increase tree mortality in the mixed-conifer forests of Sierra Nevada, California. However, microbiota living in mutualistic relations with plant rhizospheres have been found to mitigate the effects of suboptimal environmental conditions. The goal of this research is to isolate native beneficial bacteria, plant-growth promoting rhizobacteria (PGPR), that can alleviate heat stress in Pinus ponderosa seedlings. Bacteria were isolated from the rhizosphere of Pinus ponderosa juveniles located in mixed-conifer stand and further characterized for PGP potential based on their ability to produce key growth regulatory phytohormones including auxin, cytokinin, and gibberellic acid. Out of ten soil samples taken, sixteen colonies were isolated and qualitatively confirmed to produce indole-3-acetic acid (auxin) using Salkowski’s reagent. Future testing will be conducted to quantitatively assess phytohormone production in bacterial isolates. Furthermore, bioassays will be performed to determine isolates abilities to increase tolerance in heat-stressed Pinus ponderosa seedlings. Upon completion of this research, a PGPR could be utilized to support the growth and transplantation of conifer seedlings as summer temperatures continue to rise due to the effects of climate change.

Keywords: conifer, heat-stressed, phytohormones, Pinus ponderosa, plant-growth promoting rhizobacteria

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2 Extreme Heat and Workforce Health in Southern Nevada

Authors: Erick R. Bandala, Kebret Kebede, Nicole Johnson, Rebecca Murray, Destiny Green, John Mejia, Polioptro Martinez-Austria

Abstract:

Summertemperature data from Clark County was collected and used to estimate two different heat-related indexes: the heat index (HI) and excess heat factor (EHF). These two indexes were used jointly with data of health-related deaths in Clark County to assess the effect of extreme heat on the exposed population. The trends of the heat indexes were then analyzed for the 2007-2016 decadeandthe correlation between heat wave episodes and the number of heat-related deaths in the area was estimated. The HI showed that this value has increased significantly in June, July, and August over the last ten years. The same trend was found for the EHF, which showed a clear increase in the severity and number of these events per year. The number of heat wave episodes increased from 1.4 per year during the 1980-2016 period to 1.66 per yearduring the 2007-2016 period. However, a different trend was found for heat-wave-event duration, which decreasedfrom an average of 20.4 days during the trans-decadal period (1980-2016) to 18.1 days during the most recent decade(2007-2016). The number of heat-related deaths was also found to increase from 2007 to 2016, with 2016 with the highest number of heat-related deaths. Both HI and the number of deaths showeda normal-like distribution for June, July, and August, with the peak values reached in late July and early August. The average maximum HI values better correlated with the number of deaths registered in Clark County than the EHF, probably because HI uses the maximum temperature and humidity in its estimation,whereas EHF uses the average medium temperature. However, it is worth testing the EHF of the study zone because it was reported to fit properly in the case of heat-related morbidity. For the overall period, 437 heat-related deaths were registered in Clark County, with 20% of the deaths occurring in June, 52% occurring in July, 18% occurring in August,and the remaining 10% occurring in the other months of the year. The most vulnerable subpopulation was people over 50 years old, for which 76% of the heat-related deaths were registered.Most of the cases were associated with heart disease preconditions. The second most vulnerable subpopulation was young adults (20-50), which accounted for 23% of the heat-related deaths. These deathswere associated with alcoholic/illegal drug intoxication.

Keywords: heat, health, hazards, workforce

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1 Experimental Evaluation of Foundation Settlement Mitigations in Liquefiable Soils using Press-in Sheet Piling Technique: 1-g Shake Table Tests

Authors: Md. Kausar Alam, Ramin Motamed

Abstract:

The damaging effects of liquefaction-induced ground movements have been frequently observed in past earthquakes, such as the 2010-2011 Canterbury Earthquake Sequence (CES) in New Zealand and the 2011 Tohoku earthquake in Japan. To reduce the consequences of soil liquefaction at shallow depths, various ground improvement techniques have been utilized in engineering practice, among which this research is focused on experimentally evaluating the press-in sheet piling technique. The press-in sheet pile technique eliminates the vibration, hammering, and noise pollution associated with dynamic sheet pile installation methods. Unfortunately, there are limited experimental studies on the press-in sheet piling technique for liquefaction mitigation using 1g shake table tests in which all the controlling mechanisms of liquefaction-induced foundation settlement, including sand ejecta, can be realistically reproduced. In this study, a series of moderate scale 1g shake table experiments were conducted at the University of Nevada, Reno, to evaluate the performance of this technique in liquefiable soil layers. First, a 1/5 size model was developed based on a recent UC San Diego shaking table experiment. The scaled model has a density of 50% for the top crust, 40% for the intermediate liquefiable layer, and 85% for the bottom dense layer. Second, a shallow foundation is seated atop an unsaturated sandy soil crust. Third, in a series of tests, a sheet pile with variable embedment depth is inserted into the liquefiable soil using the press-in technique surrounding the shallow foundations. The scaled models are subjected to harmonic input motions with amplitude and dominant frequency properly scaled based on the large-scale shake table test. This study assesses the performance of the press-in sheet piling technique in terms of reductions in the foundation movements (settlement and tilt) and generated excess pore water pressures. In addition, this paper discusses the cost-effectiveness and carbon footprint features of the studied mitigation measures.

Keywords: excess pore water pressure, foundation settlement, press-in sheet pile, soil liquefaction

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