Search results for: Chalermchai Kanchanakachain
5 Morphological Study of Trichomes in Indigofera wightii Grah. ex Wigh & Arn., Indigo Dye Species, Traditionally Used by “Thaisongdam” Thailand
Authors: Supanyika Sengsai, Aree Thongpukdee, Chalermchai Kanchanakachain
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The study aimed to collect morphological data of secretory structures that contribute to taxonomy of Indigofera. Detail features of trichomes occurrence in vegetative and reproductive organs of Indigofera wightii Grah. ex Wigh & Arn., a species traditionally used as source of indigo to dye “Thaisongdam” clothing were investigated. Examination through light microscopy and scanning electrom microscopy were done. Non secretory, T-shaped trichomes appeared throughout surfaces of stems, leaves, flowers and fruits. Secretory or glandular trichomes occurred in two types; one has big cylindrical head and short peduncle, distributed on adaxial surface of sepals and around the pedicel, whereas another possesses smaller cylindrical head but long peduncle. The latter was found on apical surface of immature pods. No phenolic and lipophilic compounds were detected from these glands.Keywords: indigofera, trichome, Thaisongdam, Thailand
Procedia PDF Downloads 3064 Compact Low-Voltage Biomedical Instrumentation Amplifiers
Authors: Phanumas Khumsat, Chalermchai Janmane
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Low-voltage instrumentation amplifier has been proposed for 3-lead electrocardiogram measurement system. The circuit’s interference rejection technique is based upon common-mode feed-forwarding where common-mode currents have cancelled each other at the output nodes. The common-mode current for cancellation is generated by means of common-mode sensing and emitter or source followers with resistors employing only one transistor. Simultaneously this particular transistor also provides common-mode feedback to the patient’s right/left leg to further reduce interference entering the amplifier. The proposed designs have been verified with simulations in 0.18-µm CMOS process operating under 1.0-V supply with CMRR greater than 80dB. Moreover ECG signals have experimentally recorded with the proposed instrumentation amplifiers implemented from discrete BJT (BC547, BC558) and MOSFET (ALD1106, ALD1107) transistors working with 1.5-V supply.Keywords: electrocardiogram, common-mode feedback, common-mode feedforward, communication engineering
Procedia PDF Downloads 3843 Effect of Tapioca Starch on Fresh Properties Concrete
Authors: C. Samita, W. Chalermchai
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This project is aimed to be a preliminary study of using Tapioca Starch as a viscosity modifying agent (VMA) in concrete work. Tapioca starch effects on the viscosity of concrete, which could be investigated from the workability of corresponding mortar. Cement only mortars with water to cement ratio (w/c) 0.25 to 0.48, superplasticizer dosage of 1% to 2.5%, starch concentration of 0%, 0.25% and 0.5%, was tested for workability. Mortar mixes that have equivalent workability (flow diameter of 250 mm, and funnel flow time of 5 seconds) for each starch concentration were identified and checked for concrete properties. Concrete were tested for initial workability, workability loss, bleeding, setting times, and compressive strength. The results showed that all concrete mixes provide same initial workability, however the mix with higher starch concentration provides slower loss. Bleeding occurs when concrete has w/c more than 0.45. For setting times, mixing with higher starch concentration provide longer setting times (around 4 hours in this experiment). Compressive strength of starch concretes which always have higher w/c, are lower than that of cement only concrete as in this experiment initial workability were controlled to be same.Keywords: viscosity modifying agent(VMA), self-leveling concrete, self-compacting concrete(SCC), low-binder SCC
Procedia PDF Downloads 2972 Study on Compressive Strength and Setting Time of Fly Ash Concrete after Slump Recovery Using Superplasticizer
Authors: Chaiyakrit Raoupatham, Ram Hari Dhakal, Chalermchai Wanichlamlert
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Fresh concrete that is on bound to be rejected due to belated use either from delay construction process or unflavored traffic cause delay on concrete delivering can recover the slump and use once again by introduce second dose of superplasticizer(naphthalene based type F) into system. By adding superplasticizer as solution for recover unusable slump loss concrete may affects other concrete properties. Therefore, this paper was observed setting time and compressive strength of concrete after being re-dose with chemical admixture type F (superplasticizer, naphthalene based) for slump recovery. The concrete used in this study was fly ash concrete with fly ash replacement of 0%, 30% and 50% respectively. Concrete mix designed for test specimen was prepared with paste content (ratio of volume of cement to volume of void in the aggregate) of 1.2 and 1.3, water-to-binder ratio (w/b) range of 0.3 to 0.58, initial dose of superplasticizer (SP) range from 0.5 to 1.6%. The setting time of concrete were tested both before and after re-dosed with different amount of second dose and time of dosing. The research was concluded that addition of second dose of superplasticizer would increase both initial and final setting times accordingly to dosage of addition. As for fly ash concrete, the prolongation effect was higher as the replacement of fly ash is increase. The prolongation effect can reach up to maximum about 4 hours. In case of compressive strength, the re-dosed concrete has strength fluctuation within acceptable range of ±10%.Keywords: compressive strength, fly ash concrete, second dose of superplasticizer, setting times
Procedia PDF Downloads 2811 Estimation Model for Concrete Slump Recovery by Using Superplasticizer
Authors: Chaiyakrit Raoupatham, Ram Hari Dhakal, Chalermchai Wanichlamlert
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This paper is aimed to introduce the solution of concrete slump recovery using chemical admixture type-F (superplasticizer, naphthalene base) to the practice, in order to solve unusable concrete problem due to concrete loss its slump, especially for those tropical countries that have faster slump loss rate. In the other hand, randomly adding superplasticizer into concrete can cause concrete to segregate. Therefore, this paper also develops the estimation model used to calculate amount of second dose of superplasticizer need for concrete slump recovery. Fresh properties of ordinary Portland cement concrete with volumetric ratio of paste to void between aggregate (paste content) of 1.1-1.3 with water-cement ratio zone of 0.30 to 0.67 and initial superplasticizer (naphthalene base) of 0.25%- 1.6% were tested for initial slump and slump loss for every 30 minutes for one and half hour by slump cone test. Those concretes with slump loss range from 10% to 90% were re-dosed and successfully recovered back to its initial slump. Slump after re-dosed was tested by slump cone test. From the result, it has been concluded that, slump loss was slower for those mix with high initial dose of superplasticizer due to addition of superplasticizer will disturb cement hydration. The required second dose of superplasticizer was affected by two major parameter, which were water-cement ratio and paste content, where lower water-cement ratio and paste content cause an increase in require second dose of superplasticizer. The amount of second dose of superplasticizer is higher as the solid content within the system is increase, solid can be either from cement particles or aggregate. The data was analyzed to form an equation use to estimate the amount of second dosage requirement of superplasticizer to recovery slump to its original.Keywords: estimation model, second superplasticizer dosage, slump loss, slump recovery
Procedia PDF Downloads 199